I finished working on the stock and hit it with a couple coats of spray paint before I went to bed this morning. You could say it's night and day difference from where I quit before. Even though it's not perfect, I'm happy with it now and that's what really counts. Like I said, I rolled up pieces of cardboard and stuck them in the 2nd and 4th holes in the stock. Then I filled the front (blue arrow) and back (red arrow) with JB Kwick. And I also put a little more where behind the 2nd hole (white arrow) so I could level it off better with a chisel, utility knife, and and sandpaper. I squared up the back end of the rib better too. The locking pin rocks front to back a little bit f I push and pull on the stock, but there's less movement in the first hole, the one I drilled through the epoxy, than there is when it's in the steel insert made into the stock. That part of it locks up tight, even better than a factory fit! So I'm not kidding when I say I'm happy with how it turned out. If I would have filled the front part with epoxy and drilled the hole first, before trying to cut the channel out, maybe I could have avoided that ugly part on the sides, between the first and second hole. That's the problem with redneck engineering. When you're doing something that has probably never been done before, you learn as you go and figure out what you should have done differently. It already had a narrow slot there for no apparent reason, other than to lighten it a tiny bit or use less material , maybe.
What do you guys think?